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HomeMy WebLinkAbout2013-02-05 Planning Board Supplemental Materials (21) d _ 44 Stiles Road °Suite One ®Salem, New Hampshire 03079 ® — TEL (603) 893-0720 - FAX (603) 893-0733 F Design Consultants, Inc. www.mhfdesign.com January 28, 2013 North Andover Planning Board 1600 Osgood Street North Andover, MA 01845 Attn: Judy Tymon, Town Planner Re: 1018 Osgood Street JFJ Holdings,LLC Sub: Response to Eggleston Environmental Review Comments Dated January 7, 2013 Dear Ms. Tvmon and Board Members: On behalf of our client, JFJ Holdings, LLC,please find enclosed a revised set of plans and supporting documentation regarding the above referenced project. The plans have been revised to address the comments in the Eggleston Environmental review letter dated January 7, 2013. Based on those comments, as shown below,we offer the following responses in bold: 1. At our meeting on 11119, we discussed the need for distributing recharge across the project site, and particularly within the Watershed Protection District. I indicated to MHF that even if there was less than two feet of separation to the seasonal high groundwater elevation, an infiltration system within the WPD should still be able to provide effective recharge and filtering of flow under most periods of lower groundwater. With the additional test pit data included in this submission, however, a clearer picture of the groundwater conditions on the site emerges, and I question whether any below-grade system can be used to effectively infiltrate storrnwater within the WPD. Seven of the eight test pits conducted on the site (four in August 2012 and another four in November 2012) indicate that the high groundwater elevation is approximately three to four feet below existing grade across the site. Evidence of groundwater was not seen in the eighth test pit, however based on the other test pits the ESHGW was estimated to also be four feet below grade. Thus, the ESHGW elevation across most of the project site ranges from elevation 144 to 140. Infiltration System #1 (near the wetland) is located in a portion of the site where the proposed ground elevation will be raised. The bottom of the stone in the system would only be 1.2 feet above the ESHGW, but the system should be able to function adequately most of the time. Proposed Infiltration System #2, however, is located in a cut portion of the site, where the proposed surface grades will be lowered by approximately three feet. The entire below-grade infiltration system, with a bottom invert of 136.67, would therefore be several feet lower than the ESHGW elevation in that area, and likely to be in groundwater most of the year. ENGINEERS 0 PLANNERS SURVEYORS Ms.Judy Tymon January 28,2013 Page 2 of 3 MHF Design Consultants,Inc. Response: Additional test pits have been performed on 1/28/13 and added to the Flan Set and Stormwater Deport and the results provide consistent data with the previously submitted logs. Please note that infiltration system #2 has been raised two additional feet compared to the previous design. In addition,the results of'fest Pit 9113-4 indicate a depth to eshwt of 6', thereby providing the required 2' of separation to the eshwt to proposed infiltration system #1. 2. Even without the groundwater issue, the proposed plan only attenuates the rate of runoff flow leaving the site, not the volume. The volume of flow discharged to Osgood Street under post-development conditions would more than twice the existing runoff volume under every design storm condition, and could exacerbate any downstream flooding. Response: We have increased the volume capacity within both infiltration systems to the maximum extent based on the existing site conditions. In order to mitigate the Post Development volumes the onsite infiltration systems would need to be increased in upwards of 5-10x the size of the currently proposed system and in our opinion is unreasonable and inconsistent with previous developments approved in'Town. 3. The proposed design also does not provide sufficient dead storage volume in the infiltration systems to capture and treat even a %2-inch water quality volume. The TSS calculations submitted include storage volume in the Oil/Grit Chambers to reduce the water quality volume in the infiltration systems. This is an invalid assumption for two reasons. First, the oil/grit chambers are solid structures and are designed to operate full and to remain full between storms — they have no storage capacity. Second, the treatment provided in the infiltration system is only in the flow that is actually captured and infiltrated; the overflow from the system is not treated. Therefore in order to get the 80% TSS removal credit the entire water quality volume must be captured and infiltrated. Response: Storage volume within both infiltration systems has been increased to treat the 1/2-inch water quality volume. 4. It is not clear what the basis is for the saturated thicknesses of 129 and 133 ft used in the mounding calculations. As indicated in my previous comments, saturated thickness should be the difference between ESHGW and the bottom of the aquifer, probably something in the range of 10 to 15 feet. The model may call for an elevation, but it also needs the relative elevations as the saturated thickness of the aquifer is part of what determines how quickly the additional groundwater flow is dispersed. The elevations used in the analysis are not even consistent with the ESHGW on the site. Response: The saturated thickness was taken by subtracting the 10 to 15 feet from the ground surface elevation at each test pit location in the vicinity o each infiltration system. This has been revised by subtracting the 10 to 15 feet from the eshwt as suggested. Ms.Judy TymonEMUSINNumaw NINE=, MW BMW January 28,2013 Page 3 of 3 _ P HF Design Consultants, Inc. 5. The detail for the Snout Oil/Water separator on Sheet 8 should be clarified or relabeled to indicate that it is the outlet hood for the catchbasins, so as not to confuse it with the detail for the larger oil/water separator chambers. 1 would actually suggest that the larger chambers be called out as oil-grit chambers. The detail for the Stormceptor units should also be removed from the plan. Response: The detail for the Snout Oil/Water separator has been relabeled as suggested and the Stormceptor unit details have been removed from the plan set. 6. An application for a Watershed Special Permit, including a written certification by a professional engineer stating that the project will not cause any significant degradation in the quality or quantity of water in or entering Lake Cochichewick is still needed. Response: Written certification has been provided as suggested. Eased on the revised plans and documents,we feel that we have addressed the comments in both the review letter and the staff meeting. Please contact our office if you have any comments or questions. Sincerely, I) sign Consultants,Inc. is A Tymula - Project Manager F:\Projects\Eng\305311\EE Review--Response 1-28-13.docx cc: Lisa Eggleston, Eggleston Environmental Greg Nolan, JFJ Holdings, LLC